I’m a bit flummoxed: I don’t know how this happened or for that matter, how to fix it. Prior to covering, the tail was bolted on and the controls rigged. As supplied, the bushings in the stabilizer ribs holding the elevator trim crank rod were not quite perfectly aligned. This must have been due to minor warping of the steel ribs during welding. Small tweaks and twists of the ribs had the rods turning smoothly and easily. I lubricated the bushings well with white lithium grease (pictured), attached the control horns to the rods and proceeded to cover.
After the stabs were covered I notice considerable tightness in the bushings. It’s very difficult to rotate the rods, whereas it was easy before. There isn’t any particular point where there is acute binding, just generally high friction. I am unable to remove the rods easily because Mark G suggested that I both bolt and JB weld the control horns onto the end of the rods in order to prevent slop. I can move them laterally the width of the control horn slot (about an inch) which I have done to re-lubricate, without success. There is no corrosion evident. No glue entered the bushings. I also tried 5-20 synthetic motor oil, without any noticeable improvement over the white lithium grease. Temperature in my shop is between freezing and 55 F. Since covering it has been bell below freezing for several weeks.
Has anyone else experienced this issue, and if so, what did you do about it? I’m supposing that maybe the shrinking of the covering might have displaced the ribs ever so slightly, which in turn misaligned the bushings. It’s weird though, because the rods were in position in the bushings throughout the covering process. Another concern is if I tear the covering off and do it again, I assume the same issue will present again. Appreciating in advance any comments. IMG_0099.jpg IMG_0100.jpg
After the stabs were covered I notice considerable tightness in the bushings. It’s very difficult to rotate the rods, whereas it was easy before. There isn’t any particular point where there is acute binding, just generally high friction. I am unable to remove the rods easily because Mark G suggested that I both bolt and JB weld the control horns onto the end of the rods in order to prevent slop. I can move them laterally the width of the control horn slot (about an inch) which I have done to re-lubricate, without success. There is no corrosion evident. No glue entered the bushings. I also tried 5-20 synthetic motor oil, without any noticeable improvement over the white lithium grease. Temperature in my shop is between freezing and 55 F. Since covering it has been bell below freezing for several weeks.
Has anyone else experienced this issue, and if so, what did you do about it? I’m supposing that maybe the shrinking of the covering might have displaced the ribs ever so slightly, which in turn misaligned the bushings. It’s weird though, because the rods were in position in the bushings throughout the covering process. Another concern is if I tear the covering off and do it again, I assume the same issue will present again. Appreciating in advance any comments. IMG_0099.jpg IMG_0100.jpg
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