Many of us with an IO540 or similar weight engine up front experience loss of elevator authority at low airspeeds when at reduced thrust and in the forward CG range.
Kevin D mentions a potential fix on this thread HERE :
I thought this would be a very interesting discussion. Has anyone else made similar adjustments? Can we collate the results on this thread ? If there is a way to reduce or eliminate this issue then it would benefit all of us.
Kevin D mentions a potential fix on this thread HERE :
Then I lowered the horizontal leading edge about 3/16 of an inch after installation of tail VGās no stability degradation but notable improvement in low speed elevator authority.ā
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