Phase one flight testing. I am following the EAA Flight Test Task Based. But that program by the letter does not address Engine Break-in. So when Engine break-in is complete, then the program gets implemented in earnest. The first flight was about 45 minutes with the goal of running the engine hard and returning to check things over for pending infant mortality issues.
Issues we found in flight
-Prop RPM needs adjusting
-Rigging - needs slight left rudder in cruise, and has slight L heavy wing.
-ADS-b failed to record anything.
-IAS seems to read slow ~ 10 kts.
The next two flights were dedicated to fixing ADS-b issue as the aircraft is based in ADS-b airspace. This was fixed thru adjustment of settings of the Trig Transponder. In those two flights a ground test found that Prop low pitch stop was set perfectly by Hartzell and so a govenor adjustment was made. The rudder rigging is being addressed. Once that is good, we will address the roll rigging. A trim tab is commonly installed to fix this.
With my focus on Engine Break-in I am not spending much time playing with stuff at various airspeed, then stopping, adjusting, then seeing what effect it has. I flew a 2+ hour flight yesterday and do one thing at a time. I am also going to test out a simple rudder trim device that uses an adjustable bungee to apply some rudder pressure. This is what my colleague calls a MPV design.... "Minimally Viable Product".
Airspeed. The pitot/static tube I installed is from Steen Aero Lab. It sticks out about 10" from the leading edge. We are getting low airspeed readouts....Data says about 14 kts slow. The Husky has a very very similar pitot static tube and they have had the same issue and have a fix for it. I am on there group and getting some good data/ideas that we will implement to improve the error. I might end up getting it fixed with modifications to the pitot tube or move the static port to the fuselage. Right now I see 97 KTAS on the Garmin G5. When I fly a GPS box pattern and average the speed of the four legs I get 111 kts ground speed. I think the compression of the air as it runs into the leading edge of the wing is increasing the pressure at the static holes in the probe, so the airspeed reads low. I will play with various treatments ahead of and behind those holes just aft of the pitot tube "nozzle" and see what happens.
Screenshot 2025-02-25 at 7.43.28 PM.png
Issues we found in flight
-Prop RPM needs adjusting
-Rigging - needs slight left rudder in cruise, and has slight L heavy wing.
-ADS-b failed to record anything.
-IAS seems to read slow ~ 10 kts.
The next two flights were dedicated to fixing ADS-b issue as the aircraft is based in ADS-b airspace. This was fixed thru adjustment of settings of the Trig Transponder. In those two flights a ground test found that Prop low pitch stop was set perfectly by Hartzell and so a govenor adjustment was made. The rudder rigging is being addressed. Once that is good, we will address the roll rigging. A trim tab is commonly installed to fix this.
With my focus on Engine Break-in I am not spending much time playing with stuff at various airspeed, then stopping, adjusting, then seeing what effect it has. I flew a 2+ hour flight yesterday and do one thing at a time. I am also going to test out a simple rudder trim device that uses an adjustable bungee to apply some rudder pressure. This is what my colleague calls a MPV design.... "Minimally Viable Product".
Airspeed. The pitot/static tube I installed is from Steen Aero Lab. It sticks out about 10" from the leading edge. We are getting low airspeed readouts....Data says about 14 kts slow. The Husky has a very very similar pitot static tube and they have had the same issue and have a fix for it. I am on there group and getting some good data/ideas that we will implement to improve the error. I might end up getting it fixed with modifications to the pitot tube or move the static port to the fuselage. Right now I see 97 KTAS on the Garmin G5. When I fly a GPS box pattern and average the speed of the four legs I get 111 kts ground speed. I think the compression of the air as it runs into the leading edge of the wing is increasing the pressure at the static holes in the probe, so the airspeed reads low. I will play with various treatments ahead of and behind those holes just aft of the pitot tube "nozzle" and see what happens.
Screenshot 2025-02-25 at 7.43.28 PM.png
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